The Rest of the Issues Resolved

The cooling system issue resolved by two actions - had radiator flushed and repaired professionally and installed a Macy's Hurricane Fan blade for increased air flow.  Now runs really cool, also confirmed by a new temperature gauge.

Can was still not quite running right.  After putting more miles on it, decided the carbs were just not set right.  Turned out we had the wrong combination of jets and needles - jets were too big (0.100 inch) for the correct needles we had.  Thanks Joe Curto for the advice that led to this discovery!  Got the right jets in and runs MUCH better.  New points and condenser plus plugs also helped.  

Got around to installing the rear panel and floor carpet in the trunk, looks much nicer:



We decided to wait on marketing the car until Spring, convertibles not being as exciting during the winter months.  Meantime Ray and I worked with our local car club SIR Brit to bring a 1971 TR6 back to life - was a very successful project, and it's now gone to a new owner in Alabama.

We are now confident of having a great running TR2 that we are proud of.  It's not perfect, but it's an extremely nice looking and running rare early TR2.  We look forward to the new owner enjoying a great ride!

Comments

Popular posts from this blog

Good Progress for First Week

New Project Car

Fettling